Wrong value for MAIN_ON

pull/155/head
Ted Slesinski 7 years ago
parent 13145dd9a7
commit 791a440709
  1. 2
      selfdrive/car/honda/carstate.py

@ -291,7 +291,7 @@ def get_can_signals(CP):
("BRAKE_ERROR_1", 0x1b0, 1),
("BRAKE_ERROR_2", 0x1b0, 1),
("GEAR_SHIFTER", 0x1a3, 0),
("MAIN_ON", 0x1a6, 0),
("MAIN_ON", 0x326, 0),
("ACC_STATUS", 0x17c, 0),
("PEDAL_GAS", 0x17c, 0),
("CRUISE_SETTING", 0x296, 0),

Loading…
Cancel
Save